BusyBee FPV. Add gyro to increase roll stability as it is quite windy in winter. Motor mount modified to adapt 1080 propeller. With a 1000kv /3s setup, current is 16A with thrust > 600g.
Test flight for 2 times and quite satified with the gyro, which is dial down to less than45%
All electronics on board are submerged. Miracally, only the receiver and motor (killed by the receiver commanding full throttle , but kinked) is toasted. ECS, UBEC, gyro and servo are intact after H2O treatment. Lipo is overdischarged, due to internal short circuit to 3.3V/2.6V/ 1.5V. Slow recharging at 300mA brings it to life, but need further high current loading test to confirm re-usability.
Due to the NW monsoon and water current, it drifted to almost 2km away from the crash point in 1 hour. Finally I can fetch it with fishing wire .
Thanks Mr. fisherman to help me catching the plane with his fishing wire. He is so happy to catch a large fish that morning.